Hello,
If this has been answered already I apologize, I could not find a similar issue in other posts.
I've assembled and tested my kit, and it was working properly, but now it seems one servo output is not working- in calibration mode it never moves. To confirm my suspicion that the board servo output port is bad, I did the following:
Checked connector mate is good pins: on Nyboard (v 1.2) look good.
I tested the servo that wasn't working by plugging it in another port, it moved as expected.
Tried another known good servo in the bad port.
Is there any other steps that could be done? Could I get a replacement board? I've only had the device assembled and working for a few days.
Thanks,
Pete
Hi,
You have tried good methods to debug. Here's a complete routine to locate the problem: https://docs.petoi.com/technical-support/faq-frequently-asked-questions#the-robot-servos-dont-seem-to-be-working.-how-to-debug-the-servos
There's a spare servo in the package for timely fix. Meanwhile, please write to support@petoi.com to request a replacement.